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高桩梁板码头晃动原因分析及处理对策
引用本文:徐卫军,雷国刚,厉泽逸.高桩梁板码头晃动原因分析及处理对策[J].水运工程,2011(2):58-62.
作者姓名:徐卫军  雷国刚  厉泽逸
作者单位:1. 长江勘测规划设计研究院,湖北,武汉,430072
2. 南京市水利建筑工程总公司一公司,江苏,南京,210036
摘    要:某高桩梁板码头在运营过程中出现明显的晃动现象。采用三维有限元数值动力分析方法,取码头的1/2排架系统计算结构的自振频率,采用m法模拟桩周土对桩的约束作用,用ANSYS程序进行计算分析不同处理措施下码头第一振动频率的提高值。计算分析表明:采取抛石固桩、桩内灌注混凝土和增设钢撑后,码头第一振动频率提高10%~84%,能有效解决码头晃动问题。

关 键 词:高桩码头  排架  斜桩  晃动  振动响应  自振频率

Sloshing reasons and treatment measures of beam-slab piled wharf
XU Wei-jun,LEI Guo-gang,LI Ze-yi.Sloshing reasons and treatment measures of beam-slab piled wharf[J].Port & Waterway Engineering,2011(2):58-62.
Authors:XU Wei-jun  LEI Guo-gang  LI Ze-yi
Institution:XU Wei-jun1,LEI Guo-gang2,LI Ze-yi1,(1.Changjiang Institute of Survey,Planning,Design and Research,Wuhan 430010,China,2.First Company of Nanjing Water Conservancy Construction Corporation,Nanjing 210036,China)
Abstract:A beam-slab piled wharf appeared sloshing in the process of operation.Using three-dimensional finite element analysis,we computed the natural frequency of a half of the wharf bent system,simulated the restraint function of soil effecting piles by m method,and analyzed the wharf's first vibration frequency about different treatment measures by ANSYS software.The calculating and analyzing results show that through rubble filling,concrete pouring into the pile,and welding of steel pipe on the wharf bent,the fi...
Keywords:piled wharf  bent  inclined pile  sloshing  vibration response  natural frequency  
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