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沙河水库主坝泄洪闸水力模型试验研究
引用本文:李菲菲,何萍,陆雯.沙河水库主坝泄洪闸水力模型试验研究[J].南通航运职业技术学院学报,2010,9(2):78-82.
作者姓名:李菲菲  何萍  陆雯
作者单位:1. 上海友为工程设计有限公司,设计部,上海,200333
2. 扬州大学,水利科学与工程学院,江苏,扬州,225009
摘    要:文章采用整体模型试验研究方法,测试沙河水库主坝泄洪道在原有设计尺寸和变更一级跌水池长的情况下,水流流态、消能率及跃后长度的不同情形,得出将一级跌水池增加4m、扩散段相应地缩短4m时水流形态及消能效果最佳的结论。

关 键 词:整体模型试验  跌水池  消能率  水面线

A Experimental Study of Hydraulic Model of Dam Flood-discharge Gate of Shahe Reservoir
LI Fei-fei,HE Ping,LU Wen.A Experimental Study of Hydraulic Model of Dam Flood-discharge Gate of Shahe Reservoir[J].Journal of Nantong Vocational & Technical Shipping College,2010,9(2):78-82.
Authors:LI Fei-fei  HE Ping  LU Wen
Institution:1. Dept. of Design, Shanghai Youwei Engineering Design Co. Ltd., Shanghai 200333, China;2.School of Hydraulic Science and Engineering, Yangzhou University, Yangzhou 225009, China)
Abstract:Based on the integral model experiment, the different conditions of the main dam’s flood-discharge gate of Shahe Reservoir in terms of the flow state, the ratio of energy dissipation, and the length after plunge are tested in the context of original size and altered length level of plunge pool, and the conclusions that the optimal result of flow state and energy dissipation could be achieved in the situation of the plunge pool extended by four meters and the diffusion length shortened by four meters accordingly are drawn as well.
Keywords:Integral model experiment  Plunge pool  Ratio of energy dissipation  Water surface profile
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